Mery Explosive Engine - page 2
It occurred to me that to the casual reader, these operations may seem broken or out of order. Sometimes an actual size on one part may have a bearing on another. For example, it's more difficult to bore the cylinder than it is to turn the piston, so by boring the cylinder first, if I'm off a thousandth or so, I can adjust when I turn the piston. It's this thinking ahead that can keep you out of trouble. Sometimes I also just need to put a piece aside and work on something else while I think of how I want to do the next operation.
 			
			
			
Here is the drilling operation in the base for the cylinder bolt 
			holes.  I hung the base off the back of the table while the 
			front of the base was clamped to an angle plate.  Because of 
			this, I had to swing the head over to the part.
 			
			
			
Here 
			is the setup for cutting the bearing ends.  My table travel 
			wasn't long enough to allow me to edge find the actual bore so I 
			centered using the scribe line on the back of the part.  I 
			checked how close I was to the bore center afterwards and it was 
			.003" off center, way close enough.  Just 
			because it might come in handy I took a skim cut on the top face to 
			level off the sides of the housing.  I still have to drill the 
			holes in the bottom for the base and this gives me something to set 
			down on.  After cleanup and paint it won't show.
 			
			
			


Drilling 
			and boring for the crankshaft.  Rather than drilling the second 
			crank hole straight through, I used a long center drill to locate it 
			in case the drill walked.  The quill feed was a bit too loose 
			to bore with so I used table up feed.  I also cut the end of 
			the countershaft section. The countershaft hole has a critical 
			location of 3.125 from the center of the crankshaft because of the 
			gear mesh. The other dimensions aren't critical because they involve 
			the eccentric rods that can have the length adjusted.  So to 
			find the 3.125" I used the protractor to roughly find the angle.  
			It's about 40deg so getting out the trig book gave me the 'up' and 
			'over' dimensions for the hole.  Then I flipped it over and cut the other 
			end of the countershaft section.
 			
			
			
Now 
			that I have the exact 'as built' diameter of the casting crank bores, I can 
			make the bearings.  A piece of 1" brass cut in half then flats 
			milled on the back and the mating surfaces milled clean as a pair 
			puts the split centered on the back flats.  Soft solder the 
			halves together and setup in the 4 jaw indicating on the flats.
 			
			
			



Now 
			the fun part.  The crank is a piece of 5/8" by 4" CRS.  I 
			laid out the rough lines on it and had to saw it the long side for 
			width.  Then I milled it to length and drilled the ends on 
			centers for the shaft and the throw.  I then drilled a hole and 
			sawed out the chunk where the throw would be cut.  This is 
			easier than trying to turn it out for hours listening to chunk, 
			chunk in the lathe.  You can't take large cuts in this type of 
			setup.  So now it's on to the lathe.  Mounted between 
			centers, turn the throw first.  Little by little until you get 
			to about .010 all around.  I then finished the sides with a 
			radius nosed tool (pic4).  Next I radius ground the 3/32 
			parting tool and turned the diameter a couple thousandths at a time.  
			I had very small steps in the corners because of the radius mismatch 
			but a jewelers file made quick work of that.  Then a bit of 320 
			grit and 400 grit and that part is done.  Oh, don't forget 
			about the back end radius show on the top of the part in pic5.  
			Notice in pic3 the 1,2,3 blocks looking useless?  Can you say 
			counterbalance?  BTW, I only ran this at 220 RPM.
 			
			
			
The 
			above group of pictures is cutting the throw.  The first 
			picture here is after cutting one of the shafts on the band saw and 
			still turning a rough cut between centers.  I left it about 
			.015" large on both the diameter and the throw side.  I didn't 
			get a shot roughing the other side but it was the same, band saw the 
			large piece and rough turn to .015" large.  I did start turning 
			finish dimension between centers but toward the center I started to 
			chatter because of the off balance throw.  I was turning at 
			600RPM.  I ended up finishing the crank in a 3 jaw chuck.  
			By turning the majority between centers, any stress bowing was taken 
			out but I still chucked it at the end of the shaft instead of 
			grabbing it right up against the throw.  The second shot is 
			cutting the throw side to finish.  Once I had that, I went back 
			to the shaft to cut the final .005".  Finished dimension for 
			the shafts is .4995".  I turned to .501" and used 320 then 400 
			grit to polish off the last bit to size.  Two things to note: I 
			turned a chunk of aluminum to exactly fill the gap of the throws so 
			the pressure of the center didn't bend them.  It's held in 
			place with (don't laugh) wood glue.  The wood glue sticks 
			enough to hold it from falling out without the pressure of the 
			center but cleans up easily and isn't brittle.  Also, note the 
			indicator in the second shot lower left.  That's how I repeat 
			working to a shoulder.  You don't need a fancy digital readout 
			to work accurately.
 			
			
			
Once 
			I started to get close to final diameter I noticed I was turning a 
			taper of about .001".  I could live with it and compensate for 
			it with emery paper later or I could fix it.  Sometimes people 
			over think resetting the tailstock.  In my case that was the 
			cause of the taper, it was off center.  I took the indicator 
			off the mag base and chucked it.  Now by spinning it around the 
			center I was able to indicate in the center so I had about a .0002 
			taper.  I think I'll start another section on hints and tips 
			for this kind of thing to help others that are just starting.
 			
			
			
I 
			had 2 options for making the crosshead shoes; I could turn a round 
			piece to 1.500" and cut out the shoe parts then mill the back of a 
			semi round part OR mill the shoes out of bar stock and bolt them to 
			the crosshead and turn them.  By doing the later, it's much 
			quicker, more accurate and it's concentric to the 1/4-28 thread.  
			They are only held on by one 4-40 stud so I cheated a bit and added 
			a drop of epoxy when I bolted them to keep them from moving while I 
			turned them.  Next, I drilled the tapered pin hole.  I 
			reamed it with the taper pin reamer but only to the point of getting 
			the taper in both sides.  I didn't ream to depth.  It's 
			easier to finish the depth when the pin is done.  The reamer is 
			fine tuning.
 			
			
			

The 
			crosshead pin needs two sections tapered and a section in the middle 
			straight.  Oh, and a threaded section...  Take it one step 
			at a time.  Before you do anything, set the taper.  Taper 
			pins are tapered .250" per foot.  That comes out to .0208"per 
			inch.  PIC-1 is a straight shaft with marks at one and two 
			inches.  I swiveled the cross slide to 1deg and started there.  
			You want the indicator to show 1/2 of the .0208" or .0104" per inch.  
			The longer you can indicate, the closer you can get to correct.  
			I eventually went to 3".  That's .0312" for the whole 3".  
			Try for less than .0005" error.  Now turn the straight section 
			first.  Add up the threaded section, the small tapered section, 
			and the threaded section and that's the length of the .281" to turn.  
			Now turn the threaded section and thread.  Now for the taper.  
			Start cutting that, your goal is to have the tapered sections .187" 
			wide, that's all.  Don't worry about diameters, the finish ream 
			by hand will walk that right in for you.  In the second and 
			third pics are the crosshead pushed on the taper lightly with marker 
			ink on the shaft.  The third pic is the crosshead pulled off a 
			bit showing the taper contact on both sections.  If you're not 
			sure of your taper, turn a practice piece.  The better your 
			taper, the less chance of that pin coming loose later.  Don't 
			be afraid of using a bit of 320 grit to help the fit.